Daytec's Swing Arm Installation - The Cure For High Speed Wobbles

01. We had just blazed up I-15 from the fog-choked Los Angeles basin into the bright sunsh
We rolled out of foggy, drizzly Los Angeles early Tuesday morning on our way to Daytec Center "up the hill" in Hesperia, California. We had run into Phil Day a few weeks earlier and he informed us of his "cure" for the high-speed wobbles that dressers have been plagued with for many years. Craig Murrow, one of our ad sales associates, has a '01 Twin-Cam dresser and he was one of the parties listening to Phil describe the cure. Craig has ridden his bike to Sturgis and back the last 4 or 5 years and has had first-hand experience on the dreaded wobbles that start at about 85 miles an hour. "You can drive through them (wobbles) if you stay on the gas," he said. But not all riders have that kind of confidence to "stay on the gas." It would be much easier to fix the problem. That's why we were cold, wet, and heading up the hill to Daytec.
As we crested the summit of the Cajon pass the sun breaks and through the clouds, the scenery lit up and the temperature rose. As we threaded our way through Hesperia, we thought of watching the rear of Craig's bike as we motored up the hill. While his bike did not break out in any wobbles, the back end certainly did some serious shimmying around--especially on some of the high-speed sweeping turns. This led us to believe the ride back down the hill would be interesting, providing we got out of town while there was still some light. But true to Phil's word, Craig had a whole new bike; a much more solid bike. As we came down the hill after being at Daytec all day, Craig had a grin on his face that would have taken a 2x4 to remove. There was one small problem: The whereabouts of a bare wire that no one spotted or even looked for while the bike was on the lift. We did, however, see signs of that wire on the way down the hill with a few episodes of the bike shooting sparks out from underneath. The reason or cure for the ill handling or "bagger wobbles" is not one thing alone. It is a combination of many small items that when present altogether, make for a handful of a machine at any speed above the posted limit. The main component of the cure from Daytec is the company's robust swingarm. The stock swingarm, which is constructed from rectangular tubing, will twist under strenuous circumstances, thus contributing to the wobbles. Installing a Daytec swingarm in addition to the following procedures developed by Phil Day will make your bike solid under any road conditions and speed. But like we said earlier, the cure is a combination of little adjustments done in the correct sequence using quality parts. Quality parts include the swingarm with a new 1-inch diameter axle and new isolator mounts for the swingarm, as well as a new turnbuckle adjuster for the front and the rear of the bike.
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02. Once inside the R&D shop, Phil and Aaron, who you'll see soon enough, got to work tear
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03. The new Daytec swingarm, already powdercoated along with a new set of swingarm mounts,
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04. Craig's bike was rolled over to the lift and positioned so the framerails would set be
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05. Here, Phil Arlotti (A) is making sure the bike is sitting square so it can be secured
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06. The bike was positioned properly and parts started to come off, like the exhaust and w
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07. One of the fascinating aspects of Daytec is the tool boxes. Every special tool Phil de
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08. With the front wheel and brake removed, the first pieces of the alignment tooling were
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09. What Phil and Aaron were leading up to is a system to check the alignment of the wheel
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10. Here, Aaron is removing the rear wheel and shock absorbers in preparation for the rear
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11. With the wheel and shocks out of the way, Aaron fitted the rear hangers for the alignm
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12. The rear axle was placed back in the swingarm through the axle adjusters and the rear
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13. To start the evaluation/measuring process, the first order of business was to level th
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14. The frame needed to be adjusted to bring it level. Phil is turning a bolt (A) threaded
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15. Now that the frame was level, Phil checked the level of the rear tooling by placing th
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16. Now that the frame and rear tooling was level, Aaron used a set of trammel points to c
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17. The front tooling has been leveled and the strut was locked down. Next, Aaron and Phil
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18. The initial measurements have been completed. Phil has determined that Craig's bike wa
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19. With the knowledge that the chassis was off a slight amount (this slight amount can be
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20. On rubber-mount bikes, the swingarm pivot bolt locates the rear of the drivetrain as i
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21. Even after Aaron has removed all of the mounting bolts, it still required a certain am
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22. The old (A) and the new (B) isolators are the mounts that allow the driveline to move
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23. Here is the back of Craig's bike with the swingarm, mounts, and pivot shaft removed. H
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24. While Phil and Aaron worked on the bike, Craig wanted to change out his rear pulley an
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25. Aaron proceeded to strip the primary drive from Craig's bike. Here, he's pulling the i
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26. Ah ha! Here is the source of Craig's problem spotting the shop floor back at the offic
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27. Phil Day devised a way to make the primary's oil tight by O-ringing the bolt holes tha
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28. After the inner primary got a thin coat of Halomar and a new main shaft seal, Aaron wa
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29. While Aaron was working on the primary, Phil was over at the machine shop having Craig
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30. Back over on the primary side, Aaron was just about ready to button up. Here, he appli
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31. The new Daytec swingarm comes with the new bushings installed and requires some finess
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32. The swingarm pivot bolt was coated in Never-Seize--the copper variety--and pushed (by
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33. We're on our way getting things back together. The swingarm was in place and torqued t
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34. Here, the rear tooling is now assembled on the new swingarm. The axle adjusters have b
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35. Going back to the frontend, Aaron again checked it for level. All of the pulling and p
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36. Aaron had the trammel points out again and was insuring that the rear axle was paralle
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37. After the rear axle and pivot bolt were aligned and parallel, Aaron and Phil checked t
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38. Phil is removing the front engine-mounting bolt so that he can adjust the front to rea
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39. The front stabilizer link (A) is used to adjust the front to rear axle measurement. By
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40. To bring the front motor mount into line where it won't load, Phil loosened the bolts
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41. The next measurement is the vertical alignment. This is controlled by the top stabiliz
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42. One of the last items to deal with at the rear of Craig's bike is the rear fender. The
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43. There is something to be said for measuring two or three times but only cutting once.
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44. While Aaron was slicing and dicing the rear fender, Phil and Craig were fitting the fr
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45. The shocks that Craig had fitted to his bike would not work with the new stiffer swing
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46. Now we're on the downhill side of this project. At this point, Craig's bike is coming
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47. For the rear wheel install, Aaron once again used the uprights and the scissor jack to
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48. The last measurement with the trammel points is to make sure the rear axle is parallel
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49. With the rear axle torqued to 100 lb-ft (new 1-inch axle) the chrome axle covers (arro
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50. Aaron is showing some teeth as he and Phil reassembled the Bassani exhaust system. The
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51. As Aaron rolled Craig's bike off of the lift, Phil Day came by the R&D shop and gave u
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52. The moment of truth; the test ride. Craig left the Daytec Center and headed down the r
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